its been a while since iv been here... but thats a story for another post.
while others would have binned it or fitted another engine, i felt that trying to keep original engine was better as i know its history and its been trouble free, fitting a 2nd hand engine would have met that i would have lost the SB3 cams or it would have had to have the head off to rework the head for the cams anyway.
i picked it up on the 5/12 and 30 miles into the trip back home the EML came on, and after stopping at warwick services, cos i decided to take the long way home, the car wouldnt let me in... because the outer door cable snapped.
the cable was fixed the next day with a 2nd hand one i acquired some time back.
i rang rob on the monday and told him that it drove fine all the way home and that the EML came on with the code relating to 'cat efficiency below threshold'. he suggested to get a spacer to space the downstream O2 sensor, which i bought and it did help with the EML but the CO emissions are still high as i had them tested today.
its going back to the place that fit the exhaust, STG Performance, next month for a larger cat fitting, in the hope that it will bring the CO levels down.